• IP addresses are NOT logged in this forum so there's no point asking. Please note that this forum is full of homophobes, racists, lunatics, schizophrenics & absolute nut jobs with a smattering of geniuses, Chinese chauvinists, Moderate Muslims and last but not least a couple of "know-it-alls" constantly sprouting their dubious wisdom. If you believe that content generated by unsavory characters might cause you offense PLEASE LEAVE NOW! Sammyboy Admin and Staff are not responsible for your hurt feelings should you choose to read any of the content here.

    The OTHER forum is HERE so please stop asking.

Korean Airlines drop in altitude from 30,000 feet to 9,000 feet a in a few short mins, 13 passengers in hospital

Franjipani

Stupidman
Loyal
Joined
Aug 20, 2022
Messages
15,359
Points
113



昨(22)日大韓航空一架載有125名乘客,從仁川機場飛往台中的KE-189班機,韓國時間下午5點多起飛後,在經過濟州島上空時,突然出「壓力系統異常」的警示。班機從3萬5千英尺,驟降到1萬英呎以下,在盤旋一段時間後,返航仁川機場。機上有15名乘客出現耳膜疼痛等症狀,迫降後有13人被緊急送醫,所幸傷勢都不嚴重。

機艙內,明顯感受到劇烈搖晃,機上氧氣罩緊急落下,乘客全都依照指示配戴,驚險畫面就發生在22日,大韓航空KE189班機,在韓國當地時間17點09分,從南韓仁川機場飛往台中,沒想到起飛半小時後,經過濟州島上空時,突然出現「壓力系統異常」警示,飛行高度開始下降,更直接從3萬5千英尺,驟降到1萬英呎以下,班機盤旋一段時間後,機長決定,折返回仁川機場,返航過程中,機上有15名乘客,陸續出現耳膜疼痛的症狀,降落後13人被緊急,送往醫院治療。

旅客王小姐說:「機艙就變很悶很熱,然後一直上下晃,然後就急速下降這樣,後來下飛機之後就有很多人送醫院。」旅客說:「耳鳴的很嚴重,然後耳朵會有啵啵啵啵的那種感覺。」受到影響的乘客,改搭23日上午10點30分的班機飛往台中,清泉崗機場,也聚集接機民眾,還有小朋友特地準備手板,給爸爸一個大大的驚喜。

旅客曾先生說:「擔心說應該是掉下來就沒救了。」旅客王小姐說:「短時間內應該也不會搭飛機。」一想到事發當下,還是心有餘悸,短時間搭飛機,恐怕還是會有陰影,而整起意外的詳細事發原因,還有待大韓航空及相關單位,進一步調查釐清。

https://tw.news.yahoo.com/韓航驚魂-飛台班機異常-驟降2-1萬英尺13人送醫-082800026.html
 
Korean Air Boeing aircraft's pressurisation system anomaly causes ear pain and nosebleeds in 17 passengers
www.dimsumdaily.hk

23rd June 2024 – (Seoul) On Saturday, a Korean Air flight operating a Boeing 737 MAX 8 aircraft had to make an emergency return to Incheon, South Korea, while en route to Taichung. The incident was triggered by an abnormality in the cabin pressurization system, which necessitated immediate action. The aircraft rapidly descended from an altitude exceeding 30,000 feet to approximately 9,000 feet, causing discomfort and health issues for some passengers.
According to official reports, at least two passengers experienced nosebleeds as a result of the sudden pressure change. Additionally, the South Korean government verified that 15 passengers complained of ear pain and excessive breathing, with 13 individuals requiring medical attention. Fortunately, there were no reports of any severe injuries among the affected passengers.
The flight, identified as KE189, was carrying 125 passengers. It departed from Incheon International Airport at 4.45pm yesterday, bound for Taichung’s Qingquan Airport. Approximately 50 minutes into the flight, while flying over Jeju Island, the aircraft’s pressurisation system issued an error report. In response, the captain made the decision to turn the aircraft around, and it safely landed back at Incheon at 7.38pm.
A Taiwanese female passenger recounted her terrifying experience on social media. She described how the plane suddenly dropped shortly after the meal service, causing intense turbulence inside the cabin. The sensation was likened to experiencing five times the gravity of a roller coaster ride, and the oxygen masks were deployed. The passenger suffered severe pain in her ears and head, feeling dizziness, while children on board began crying. The cabin crew swiftly attended to the situation, securing the meal service and distributing oxygen masks. The moment the aircraft landed at Incheon Airport, the passenger expressed relief and gratitude for being alive.
Korean Air has issued an apology regarding the incident and is actively investigating the specifics of the flight’s return to ensure necessary maintenance measures are taken. Passengers affected by the incident have been accommodated on an alternative flight scheduled for Sunday morning (23rd) to continue their journey.
bkn-20240623010222931-0623_00992_001_01p.jpg
bkn-20240623010222931-0623_00992_001_03b.jpg
bkn-20240623010222931-0623_00992_001_02b.jpg
 
Boeing 737 is extremely unsafe. Whistleblowers have given accounts of how Boeing has been reusing faulty parts. Don't fly Boeing.


https://www.dailymail.co.uk/news/ar...en-cracked-flight-Heathrow-San-Francisco.html

Packed Virgin Atlantic Boeing jet's windscreen 'cracked at 40,000 feet' on flight from Heathrow to San Francisco​

By POPPY ATKINSON GIBSON

PUBLISHED: 14:38 BST, 22 June 2024 | UPDATED: 14:46 BST, 22 June 2024


A packed Virgin Atlantic Boeing jet's windscreen 'cracked at 40,000 feet' while flying from Heathrow to San Francisco.

Photos show a dented central window pane with cracks in multiple areas but the cause of the damage has left investigators scratching their heads.

The crack in the four-layer thick glass left cockpit crew terrified as the plane made its transatlantic voyage.

The incident occurred three hours into the flight as the jet flew between Greenland and Iceland and forced Virgin Flight VS41 to make a U-turn and fly back to the UK on May 27.

Experts have said that the plane's altitude meant it could not have hit a bird and no immediate other course have been highlighted but temperatures outside the aircraft were -50 degrees Celsius.
 
So was there a loss of pressure or did the pilots over react to a warning sign?
 
There must be a reason why I always see planes flying so low even during good weather: no clouds, blue sky everywhere. And they're nowhere near an airport. :unsure:
 
https://www.taipeitimes.com/News/taiwan/archives/2024/06/24/2003819818

The flight was above Jeju Island when a fault in the pressurization system occurred 50 minutes after takeoff.

Technical fault.

Now compare this with Sinkie airline incident, when there has been no mention of any technical fault, and the SPH doggies were ceaselessly being the PR department of SIA doing damage control and spin jobs e.g. the pilot was a 'hero'. :rolleyes:
 
So was there a loss of pressure or did the pilots over react to a warning sign?
Pressurization problem. Not turbulence, not pilots' fault.
Boeing - again and again.


https://www.taipeitimes.com/News/taiwan/archives/2024/06/24/2003819818

Passengers arrive safely after scare on flight from SK

  • By Ou Su-mei and Esme Yeh / Staff reporter, with staff writer
Passengers aboard Korean Airlines Flight KE189 arrived in Taichung safely yesterday after a scare the previous day encountering uncontrolled decompression, which injured 13 passengers.

Flight KE189 departed from Incheon at 4:45pm on Saturday bound for Taichung with 125 passengers on board.

The flight was above Jeju Island when a fault in the pressurization system occurred 50 minutes after takeoff.

Online flight tracker Flightradar24’s data show that the plane dropped more than 8,000 meters within 15 minutes, before it returned and landed back at Incheon Airport at 19:38pm.

Thirteen passengers on board had a headache or earache due to the incident and were hospitalized.
 
Back
Top