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'Wow, pulled back wrong throttle' - the last words of TransAsia plane captain

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'Wow, pulled back wrong throttle' - the last words of TransAsia plane captain

Date July 2, 2015 - 11:35PM
Faith Hung

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The plane clipped an overpass and taxi before crashing. Photo: Reuters

Taipei: The captain of a TransAsia Airways ATR mistakenly switched off the plane's only working engine seconds before it crashed in February, killing 43 people, Taiwan's Aviation Safety Council (ASC) said in its latest report on Thursday.

The ASC's report also showed that Captain Liao Jian-zong, who was at the controls, had failed simulator training in May 2014, in part because he had insufficient knowledge of how to deal with an engine flame-out on take-off.

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Taiwan's Aviation Safety Council official Thomas Wang explains findings in the report released on the TransAsia Airways Flight GE235 crash in February. Photo: AP

"Wow, pulled back the wrong side throttle," Liao, 41, was heard to say on voice recordings seconds before the crash.

There appeared to be confusion in the cockpit as the two captains tried to regain control of the plane after the other engine lost power about three minutes into the doomed flight.

Liao reduced the throttle on the working engine but did not appear to realise his mistake until it was too late.

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Rescuers carrying out rescue operations from the wreckage of the TransAsia ATR plane back in February. Photo: Reuters

He tried to restart the engine before a junior first officer, who was also in the cockpit as part of his training, said: "Impact, impact, brace for impact."

Those chilling words were the last heard on the data recordings, according to the latest report of the ASC's investigation into the February 4 crash in clear weather.

Seconds later the ATR 72-600, which had 58 people on board, crashed upside down into a shallow river in downtown Taipei after it lurched between buildings, clipping an overpass and a taxi. Fifteen people survived.

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The main fuselage from TransAsia Airways Flight 235 being hoisted away. Photo: AP

A source with direct knowledge of the report told Reuters on Wednesday the working engine had been shut off. Data readings showed the almost-new turboprop ATR 72-600 stalled and crashed shortly after it was switched off.

TransAsia had no immediate comment about the latest findings but was due to hold a media briefing later on Thursday.

The council's report, which neither assigns responsibility nor suggests recommendations for improvement, paints a more detailed picture of the evidence than a preliminary report released days after the crash.

Sources familiar with the investigation have previously told Reuters the crash was probably caused by human error.


The investigation so far has shown that Liao, a former air force pilot, began to fly commercial aircraft in 2009 and joined TransAsia the following year. He was promoted to captain in August 2014 and joined the ATR 72-600 fleet in November.

He had a total of 4914 flight hours at the time of the crash, including 3151 in the ATR 72-500 and 250 hours in the ATR 72-600.

However, the report showed that Liao failed the simulator check in May 2014 when he was being evaluated for promotion. Assessors found he had a tendency not to complete procedures and checks, and his "cockpit management and flight planning" were also found wanting.

However, he passed after a second simulator check on June 29 and 30 and was promoted to captain, although similar problems were detected during training from July 2 to 10 last year.

Instructors commented at the time that he was "prone to be nervous and may make oral errors during the engine start procedure", displayed a "lack of confidence" and was "nervous", the report shows.

Issues cropped up again during training for the ATR 72-600 in November, when an instructor said Liao "may need extra training" when dealing with an engine failure after take-off.

Since the crash, Taiwan's Civil Aeronautics Administration has put all 55 of TransAsia's ATR pilots through oral proficiency tests on how to handle an aircraft during engine failure.

All but one of the pilots passed the tests, although some needed more than one attempt. The lone failure was demoted in rank to vice captain from captain.

A draft of the final report will be issued in November with the final report to be completed in April 2016, the council said. The cause of the crash and recommendations for the future will be included in the final report.

Reuters


 

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Pilot in crashed TransAsia flight shut down plane’s only working engine by mistake


Pilot in crashed TransAsia flight shut down plane’s only working engine by mistake: Taiwan probe

Official report confirms that the crash that left 43 people dead was caused by an engine malfunctioning and a pilot mistakenly shutting down the other

PUBLISHED : Thursday, 02 July, 2015, 2:37pm
UPDATED : Friday, 03 July, 2015, 1:46am

Andrea Chen and Sijia Jiang

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The airliner clipping a bridge seconds before the crash in February. Photo: SCMP Pictures

The captain of the TransAsia aircraft that crashed into a river in Taipei in February, killing 43 people, shut down the plane's only working engine by mistake after the other had failed, a report by accident investigators confirmed on Thursday.

"Wow, pulled back the wrong side throttle," Captain Liao Chien-tsung was heard saying on flight recorders eight seconds before the crash, the report by Taiwan's Aviation Safety Council said.

Liao was initially hailed a hero for steering the aircraft away from buildings.

His training records released by the council showed that he had failed a simulator check during his test for promotion to captain last year due to "insufficient knowledge" of engine flameout.

But the council did not apportion any blame in its report.

A Hong Kong-based pilot told the South China Morning Post that TransAsia had tested all pilots on the handling of engine failure since the crash and 30 per cent failed. Those who failed would receive more training and be retested. He said pilots were supposed to turn off a failed engine to secure it.

The passenger flight GE 235, an ATR72-600, clipped a bridge and crashed into the Keelung River with 58 people on board, including 31 from the mainland, just minutes after taking off from Taipei Songshan Airport.

Among the dead were the captain and the co-pilot. Thirteen passengers and one cabin crew member sustained serious injuries. The other person on board suffered only minor injuries. Two people on the ground - a taxi driver and his female passenger - suffered minor injuries.

Investigators' preliminary reports released days after the crash had suggested an engine was manually shut down after the other had malfunctioned and stopped working.

The most recent report revealed confusion in the cockpit after the dashboard warned of "flameout" in engine two about one minute after take-off.

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The captain disengaged the autopilot seconds later. "Pull back number one [engine]," the captain was heard saying while the co-pilot confirmed the other engine had suffered a flameout.

The pilots were then heard checking the malfunctioning engine and adjusting the power in the other one as the plane descended, but neither immediately noticed when the still-functioning engine shut down.

When the captain did notice, he attempted to restart the engine but failed. At this point the first officer, in the cockpit as part of his training, said: "Impact, impact, brace for impact."

Seconds later the plane crashed.

The council found Liao had performed poorly when dealing with an engine flameout during a simulator check in May 2014. He passed the test on his second attempt a month later and was promoted to captain.

His instructors described his performance during the oral exam as nervous, unconfident, and indecisive when tested on handling such emergencies.

The full investigation report will be released next April.


 
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